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Kris Walters

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Posts posted by Kris Walters

  1. The carb has been removed and cleaned by a professional.It is confirmed clean and all the passages are clean as with the jets.i still feel it's electrical/ignition that's causing the problem.One thing I have noticed is that the reverse light stays on even though the bike is not in reverse.

  2. Tore into the carb again and it is spotless,it seems like a rev limiter is causing it to act this way or weak spark.plus the whole thing with the kill switch only working backwards("run" kills it and "stop" gives spark) I posted a video of it running and me trying to rev it,but the sound quality sucks.

    Clean  the carb again. You  have a classic "running lean" problem  when you open the throttle . It  could be a plugged passage  or the  tiny drilled  holes in the  main  jet  tube,  the  idle  air screw maladjusted or possibly the float level set too  low so the float bowl  doesn't  fill  properly.  There  is a download  of the service manual  that would cover  your  machine  in the forum's download  section .
     


    Sent from my Z982 using Tapatalk

  3. So I bought this 1989 fourtrax 300 2x4 as a non running quad(no spark).finally got the thing to spark yesterday accidentally,by pushing the starter button while the kill switch was off.(I was holding the coil wire and it shocked me).so low and behold the kill switch for some reason works backwards.anyway it started up but runs terrible.it will sit and idle for as long as you let it,but as soon as the throttle is touched it boggs,and dies.thought it was a fuel issue,so I verified clean fuel source and flow from the tank.also cleaned the needle valve and jets in the carb,but that didn't help at all.if you very carefully apply throttle it will run and move but if you get past 25-30% throttle it will start popping out of the exhaust and loosing power.

    1533475759284400570871.jpg

  4. IT RUNS!!!!! Like crap,but it makes spark and starts. The issue was the CDI,and the new one I ordered from eBay was the wrong one DC I think.went to a local bike shop explained the issue and showed the box from eBay,and he immediately told me I had the wrong CDI unit.thank you fellas for all the help and input.

     

  5. Just to add more info.the previous owner stated he was riding the quad and it died.had it pulled home and began to diagnose it.the guy didn't have the proper equipment to do this so he removed the stator cover and took it to a shop for diagnosis.shop told him he had a bad stator,and tried to sell him a stator.when I got the quad I ordered a stator CDI and coil.both stators ohm correct as with the pickup/trigger coils.

  6. New to the group,please be gentle lol.So I just purchased(traded my 73 sportster) for this 1989 Honda fourtrax 300 2wd.i got the quad with a no spark condition,thinking it would be an easy fix. I have tested the stator,pickup coil,coil,and inputs going too the CDI.so far everything has tested good.while doing all this I cleaned/repaired a few dirty connections and replaced the battery and cables.the kill switch is good and the ignition switch is also good.so I ordered 3 cdiand coil kits(because I have another Honda).Tonight I put the new CDI and coil on and tried to check for spark.No spark again.but about 5 seconds after letting loose of the starter button the CDI blew apart.what am I missing here?

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