1987 Suzuki LT- 4WD
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By prdicon
I was looking to buy a new ATV.
I was debating between Polaris sportsman 450 and Honda rancher.
Polaris it a bit cheaper.
But can you tell me which one will have more demand on the used market? Which one will keep it's value better?
Let's say 3-5 years from now.
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By BillR94
I picked up this ATV that had no spark. The previous owner said he was driving it and it died and would not start. He discovered it had no spark. He replaced the CDI and the coil with no luck. He got tired of it and I bought it. I replaced the stater and now it has strong spark. Now, it starts for a second or two then dies. It will not stay running. I have checked the timing and it is spot on. The valves are adjusted correctly. I see no warn issues with the cam. I put the original CDI and coil back on it. Same problem exists. Compression is at 65 psi (has decompression mechanism),
I took off the muffler in case the issue was clogged pipes. No change. I replaced the spark plug. No change. The carb was an aftermarket so I put a Niche carb on with no change. I bypassed the fuel pump and that did nothing to solve the problem.
I don't know if this is a carb issue or an ignition issue. I am looking around locally for an OEM carb to try out but not sure that will fix the problem.
Can anyone help me solve this problem. I am running out of ideas.
Thank you for your time
Bill
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By Joeguy
After i did my rebuild it seems to not want to shift well. I think the cable is alright, and when it does shift its nice and solid. I have to basically use my hand to shift and i have to pull or push it very far, like max travel, to get it to shift. I also tried adjusting the clutch set screw. Any ideas where to go next, or maybe i should just grab a new cable to try.
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By Jason39
I’m having a issue with my choke when its on it runs fine when I cut the choke off the atv cuts off went to take the carburetor off and saw the choke plunger broke at the nut to screw it in could this be my issue? Do I just need to buy a plunger kit and put it on? I took the carburetor off and cleaned both jets anyway just to make sure and it’s still having issues staying on
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By Joeguy
Did a top end rebuild, honed .010 over, new piston, rings, valve seals, etc. When i re assembled i only had like 30 psi of compression but then after it sat all night i now it seems to have gained some somehow, there is much more resistance pulling it over and i even got it to fire for a few pops. Issue i got is that it makes a loud squeak noise through the intake i believe (goes away when throttled so something with carb area) and it seems to not want to run well. I took head cover back off and timing seems fine so im not sure if something is sticky and that's why i got some change over time or maybe the valve lash is messed up after doing all this, i did get another cam for it but i wouldnt think it would make enough difference to need to re lash. Any insight on next step would be appreciated, i will be looking up how to do lash on these because it is a very weird angle to slip a feeler gauge in.
Actually cam is slightly off now that i look at the picture, thought it was good while looking in person. Hmm.
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