Quantcast
Jump to content


Yamaha Moto 4 250 oil consumption


Diesel Dave

Recommended Posts

Hi there, I am a new member and have never used a forum before. I own a 250 moto 4, has smoked since I got it.

Oil consumption has increased, I removed the crank case breather pipe and have a catch can under frame at front. Smoke has not changed. also after more than 20 hrs use during lock down there is a very small amount of oil come out the breather.

Compression seems very high, engine turns not too bad if stopped for up to 20 mins but much more than that it is difficult to turn engine past tdc. (poss almost hydrolocked?) if left for a couple of hours or more it then turns over easier. Also if spark plug is removed. I would have expected oil to come out when turning engine with spark plug out. 

I suspect oil is getting down valve guides? smoke is worst during warm up. The starter motor has not worked since before I owned it and I have modified pull start as the pressure on it was causing problems.  I am about to check valve clearances this morning before I get going.  I do not want to dismantle while lock down is on as I am using it daily.

Any help would be greatly appreciated, Dave

Link to comment
Share on other sites

Hi there,  thanks for the reply. Spark plug looks good, I have checked the compression but only have the pull start.  I could only get a reading of 40 psi. I compared that to a Honda TRX 250 using kick start and found it was 50 psi, this one doesn't smoke.  I can't say how accurate my tester is as its an old one in my garage. I started the engine this morning, after 5-10 secs it was smoking pretty bad. I drove it for 2 mins and smoke had all but gone. I regularly keep an eye on the oil level, it requires a top up more than once a week if used daily. I have not changed the oil since owning it so will do that.  If no improvement I will have a look inside once the lock down is over. Do you have to go genuine for engine parts or can I get good after market ones online?

Cheers

Edited by Diesel Dave
Link to comment
Share on other sites

Join the conversation

You can post now and register later. If you have an account, sign in now to post with your account.
Note: Your post will require moderator approval before it will be visible.

Guest
Reply to this topic...

×   Pasted as rich text.   Paste as plain text instead

  Only 75 emoji are allowed.

×   Your link has been automatically embedded.   Display as a link instead

×   Your previous content has been restored.   Clear editor

×   You cannot paste images directly. Upload or insert images from URL.

  • Similar Forum Topics

    • By McG75
      Sorry I suck at these forums so if you see this submitted under update status, my bad. Anyhow this is a new shock for a 96 Yamaha Kodiak 400 4x4 it fits my 96 Yamaha Timberwolf 250 4x4 perfectly. Little narrower are the bottom than the original but everything else is perfect. I extended it to almost a half in from full extension because I’m pushing 350 pounds.  It rides and hold me well. So if any of y'allRace driven shock. have been looking for one and didn’t want to do the research here it is. 





    • By BruceG
      Hi guys. I have a problem where the quad will start and run well for about 5 minutes and then it dies. On inspection the airbox has oil in it (quite a lot). The oil is pumping through the cylinder head breather hose. This problem first happened suddenly. I have since done the top end including, piston, gaskets, rings and valves. I have also done the carb (not that I thought that this was the problem). The compression seems normal. The only thing that I can think of, is that I did not grind the valves well enough. Anyone experienced this? If so, how did you fix it? Any other thoughts?
    • By Mhatayas
      My uncle bought a Baja 250, 2006. Knew there was no spark since the get go. He don't know anything about quads so is getting me to help him try to get it running...
       
      battery is bad so I connected battery charger to it to crank it over , cranks over well , but no spark .... 
      Lights and everything work fine , but with each crank over using the e start switch , the display reads 999 888 777 666 ... Right down to 000 and repeats itself . 
       
      He managed to get a parts bike , I changed over the CDI and the coil and the stator from the parts bike and there was another black box by the voltage regulator I changed over ... I used my multimeter to confirm as much as I could works , it's hard without knowing which wires are which , and I cannot find any diagrams online for this bike ? 
       
      Do you think it could be the Killswitch? There's so many wires coming from there I don't know where to start . Also I should mention it appears the fan on the front of the bike has been taken off (the wires have been cut too ) 
       
      If this bike sparked it would run . The previous owner said he parked it one day and it just wouldn't start after.
    • By Mhatayas
      What should I do about this , bad oil leak where the filter cover bolts on . Can I use some gasket maker 

    • By Uglyside38
      I have a 1988 Quadrunner 250 2wd. My brother in law sold it to my son for $20...had been sitting outside for several years. Got it home and had it running in about 30 mins. Ran it a bit and then went to looking at the carb as it was having trouble idling. Was getting it pretty close, then started losing spark...Also, it wouldn't start up every time...only about 1 in 5 tries. Anyway...now, it has what I can only describe as "intermittent" spark. I can get 1 light spark right when the start button is pressed and sometimes one when it's released...but none while cranking. 🤷‍♂️

      I have replaced the spark plug, ignition coil/wire, and traced wires best I can. I noticed a couple frayed wires at the pickup coil where it enters the case. So, now I have the cover off, stator and pickup coil out and trying to test the coil. I do have about 114 ohms resistance for pickup best I can tell. And I can read minute voltage when I drag a magnet across it. Could it still be bad? Can a bad ignition switch/button cause this? (I did have the switch off to oil the choke cable)...pulling rope makes no difference though...any ideas or help would be greatly appreciated!!! It's the intermittent part that's throwing me off! 

×
×
  • Create New...